Pulled the LSX yesterday......
#31
GFYS and STFU
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Joined: Jan 2007
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From: Here and sometimes there too.
Wow, sad to see this. Makes me wonder though how long ago you lost the electrode on the number 8 plug. If you were running around on 7 cylinders for a while your 02's would of been pulling fuel on all the other cylinders causing you to run lean, somewhat explaining the condition of a few of the other cylinders but also looks like you were having problems before all that.
Those pistons were forged as well no? That crack in number 8 makes me believe you were having massive and consistent detonating if it did that to a forged piston. So I think your theory on bad knock sensors would prove to be at least in part accurate.
Those pistons were forged as well no? That crack in number 8 makes me believe you were having massive and consistent detonating if it did that to a forged piston. So I think your theory on bad knock sensors would prove to be at least in part accurate.
#35
Here's another pic of #8 after wiping it down better - droplets were just coolant. The 2 stressed areas are actually protruding humps relative to the rest of the piston face - haven't got to the bottom end yet.

Some pics of Bank 1 cylinders and head. Wiseco forged pistons appear to be intact.


Found this debris in the top side of the bank 1 head:


Some pics of Bank 1 cylinders and head. Wiseco forged pistons appear to be intact.


Found this debris in the top side of the bank 1 head:








