New MSC front mount turbo almost done!
#21
havn't noticed any real difference under partial throttle, not going full throttle till it gets the finishing touches on the tune today. don't see any reason why it should creep by routing back into a 4in exhaust.
#22
Thanks corey, but since it's an 05 it doenst have a fpr... I am running a wideband, fuel pressure gauge, boost gauge etc. It turns out I blew a head gasket, so we pulled the head off today and I was running the wrong size head gaskets for my bore( too small) lol... Some one smart did that... So that should Dix the over heat problem... Thank god for forged pistons I'm a 100% believer lol
#23
Wow, a blow head gasket... Man you don't hear about many of those with these motors... ya that should fix the heat problem... I would really clean the deck of the block and heads... Are you using stock head bolts and are you gettting new head bolts with the gaskets?
Does your fp gauge hold steady at wot?
Does your fp gauge hold steady at wot?
Last edited by BlackGMC; Oct 9, 2009 at 02:09 PM.
#25
No I have always had studded heads.. But the blew under boost because they were the wring suze head gaskets so I'm gonna have the heads and block resurfaced... What I wanna know is.. What kind of fool would put the wrong bore head gaskets on a build?? Somebody tell me the truth what's going on! Lol



