Problem getting more complicated!
#21
Originally Posted by Flyer
Sounds like the voice of experience ....
But, no. Otherwise I would have a 6.0L

I will get 500rwhp out of this 5.3L. And I am very nice to my engines...well sort of
#23
im telling you,, a leak down test would do me no good! haha. if i pump about 120 psi (the psi if my air hose) its done out the crankcase in less than a second. haha What i dont get is why im not using any oil, and not smoking, or getting any blowby if its a ring or holy piston. if it is a piston, its got to be 4 of them! flyer listened to my truck... it dont sound like 4 pistons are gone. Grrrrrrr hahaha
#25
I did see him at the track. I wouldn't have noticed it was missing unless he pointed it out ot me. There wasn't any smoke either. It actually sounded good under power too. It's definantly got me stumped. There is without a doubt something going on though, he was running 14.7 I think with the Whipple and some other mods. That is SLOW for having 6psi of boost.
#26
Originally Posted by Flyer
he was running 14.7 I think with the Whipple and some other mods. That is SLOW for having 6psi of boost.
Without some major changes, I haven't seen any whipple trucks running good times.
#29
did i mention that i retuned it back to stock tuning, and ran a 15.3 vs the 15.7 i ran bone stock from factory? that means that i only got .4 in the 1/4 with my whipple? Sorry, im still not buying it.


