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APE Project SS Silverado!

Old Sep 2, 2004 | 06:25 PM
  #71  
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Chris, Did I miss where you said what size pulley you are running? Standard measurement or metric will be just fine thanks?

The smallest I'm aware of is 2.75" but I have read some reference to a 2.7"..........

thanks in advance
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Old Sep 3, 2004 | 08:35 AM
  #72  
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2.75" diameter is what it is.
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Old Sep 6, 2004 | 01:28 PM
  #73  
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Originally Posted by Chris@AP-Engineering
Well, here are the results from the last saga of the Silverado SS! We recieved the supercharger back from Magnacharger last week and got it installed. The difference......none! Still just 5lbs of boost, but at least steady 5lbs all the time. We even ported the TB and it did nothing for the truck or boost.

So yesterday, we took the truck to W2W powertrain to use their all wheel drive Mustang dyno. They have a brand new dyno that is just awesome. After about 3 hours on the dyno here's what we came up with;
270 rwhp (the way we have been driving it)
335 rwftlbs (same as above)

These were the results after tuning!!
413 rwhp
445 rwftlbs
Still only 5lbs of boost. This truck has 400 ftlbs basically from the time you go to wide open till you get out of it!! It feels really good now, it didn't before. I still would love to have the 10lbs we were shooting for.
Well we are headed to the track tomorrow, I will let you know how it does now!!

Thanks,
Chris

I ran into the same problems with IAT with my Radix but got through it, and the most I could get out of the stock motor and radix w/ 3" pulley was 433RWHP/455RWTQ.

I'm currently building a 427 w/ a Nitrous shot.

Good luck, I hope to see more updates.....
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Old Nov 5, 2004 | 11:48 AM
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any updates/track times?
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Old Nov 5, 2004 | 12:23 PM
  #75  
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Originally Posted by O3GMC
any updates/track times?
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Old Nov 5, 2004 | 08:18 PM
  #76  
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Im also interested in seeing some new #'s as well.
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Old Nov 5, 2004 | 09:52 PM
  #77  
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Yep!
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Old Nov 7, 2004 | 04:26 PM
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Old Nov 10, 2004 | 09:06 AM
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We are looking at a few options right now. We may be ditching the Magnuson in favor of a turbo set-up. Details to follow.
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Old Nov 10, 2004 | 10:02 AM
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Originally Posted by Nick@AP-Engineering
We are looking at a few options right now. We may be ditching the Magnuson in favor of a turbo set-up. Details to follow.

Why switch it now? Why not get some track times first to get a good baseline and then switch to the turbo and see what it can do?
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