80e swap... Got a few questions.
#23
#24
#25
Update.
got the new slip yoke installed and drive shafts put back in.
exhaust is back on
dipstick tube is in (that was a PITA)
Things left to do..
shift cable braket (still in the mail)
fill trans with fluid
load new tune
got the new slip yoke installed and drive shafts put back in.
exhaust is back on
dipstick tube is in (that was a PITA)
Things left to do..
shift cable braket (still in the mail)
fill trans with fluid
load new tune
#27
finished up the swap tonight!
put 12 quarts of fluid in and it moves the truck good, it doesn't feel low or the converter too loose..
I forgot about switching the wires at the pcm, so that took a while to do.
put about 20 miles on it tonight. my tune got all kinds of screwed up when HP did the segment swap. Boost enrichment wasn't even active. so i made a quick pull at 10psi 13.00 afr
I couldn't get the converter to lock up on its own. When i commanded it with the scanner it worked fine. any thoughts
put 12 quarts of fluid in and it moves the truck good, it doesn't feel low or the converter too loose..
I forgot about switching the wires at the pcm, so that took a while to do.
put about 20 miles on it tonight. my tune got all kinds of screwed up when HP did the segment swap. Boost enrichment wasn't even active. so i made a quick pull at 10psi 13.00 afr
I couldn't get the converter to lock up on its own. When i commanded it with the scanner it worked fine. any thoughts
#28
finished up the swap tonight!
put 12 quarts of fluid in and it moves the truck good, it doesn't feel low or the converter too loose..
I forgot about switching the wires at the pcm, so that took a while to do.
put about 20 miles on it tonight. my tune got all kinds of screwed up when HP did the segment swap. Boost enrichment wasn't even active. so i made a quick pull at 10psi 13.00 afr
I couldn't get the converter to lock up on its own. When i commanded it with the scanner it worked fine. any thoughts
put 12 quarts of fluid in and it moves the truck good, it doesn't feel low or the converter too loose..
I forgot about switching the wires at the pcm, so that took a while to do.
put about 20 miles on it tonight. my tune got all kinds of screwed up when HP did the segment swap. Boost enrichment wasn't even active. so i made a quick pull at 10psi 13.00 afr
I couldn't get the converter to lock up on its own. When i commanded it with the scanner it worked fine. any thoughts
It won't lock at all on its own or it unlocks when you let off the throttle?
#29
#30
well I got the fluid level up and took it on a 60 mile trip. I locked up the converter with the scanner about 10-15 different times. took the truck out the next day and the TC started working like normal


