FORCED INDUCTION Turbos | Superchargers | Intercoolers | H2O/Meth Injection
Sponsored by:
Sponsored by:

Maybe hurt motor today

Thread Tools
 
Search this Thread
 
Old May 28, 2010 | 07:02 AM
  #1  
LBSBLOWN's Avatar
Thread Starter
TECH Apprentice
iTrader: (1)
 
Joined: May 2003
Posts: 339
Likes: 0
From: Keller, TX
Default Maybe hurt motor today

Attached is the HPT scanner file and config file, look at frame 22587 it looks a little wiered.
I was standing on it and near the top of secound gear I felt the power drop off and heard what sounded like detonation and I let up on the throttle instantly.
It seems to run fine, idles smooth and no codes, I drove easy to work and popped to hood and pulled the oil filler cap and no smoke comming out, so maybe the motor is ok, not sure yet.
But look at the scan there is no Knock retard the AFR is ok and boost is ok but all of a sudden the boost climbs to 195kpa (15psi) but the MAF airflow drops and the AFR goes up in the 14.xx"s and then i let off.

It almost looks like something restricked the exhaust like maybe a CAT melted and clogged up on the drivers side pushing all the boost to the passenger side where my WB is at.

anybody have any thoughts.

files where to big to attach so I chaned them to upload:
Change the .htp file to a .hpl scanner file to view
Change the .doc file to a .cfg config file to use
Attached Files
File Type: hpt
RX700B AT 75 DEG 29.94.hpt (888.7 KB, 76 views)
File Type: doc
LBS AFR 1 SPK IAT MPG B.doc (3.5 KB, 61 views)
Reply
Related Topics
Thread
Thread Starter
Forum
Replies
Last Post
TXsilverado
FORCED INDUCTION
48
Nov 26, 2015 10:54 AM
DrX
FORCED INDUCTION
31
Aug 19, 2015 04:45 PM
DrX
FORCED INDUCTION
4
Aug 11, 2015 07:25 AM
GRRR65GTO
INTERNAL ENGINE MODIFICATIONS
2
Jul 10, 2015 08:27 PM




All times are GMT -5. The time now is 05:47 AM.